View History
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Department
Permanent Corrective Action
Remark
Date
General Admin
Procedure of inspection modified.
Test
2023-09-02
Checklist
×
Availability of proper facility/tools/man power for boxes opening/shifting of machine to planned location
After performance confirmation w.r.t. SO - take change-over if any for further trials repeat procedure as per point no. 20 to 21
View Fault Characteristics
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Fault Characteristics
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ABC India Ltd.
15
15 Notifications
4 new messages
3 mins
8 friend requests
12 hours
3 new reports
2 days
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Demo
Demo
Call In Process / Assigned Call
763
Jalani Enterprises Private Limited.
JODHPUR
Service Call Id:
4701,
Call Created by:
Demo User,
Created On:
07-06-2024
Details
Assign Engineer
Root Cause & Final Closure
Visit Log
Machine Parameters
Competitors Parameters
Report / Documents
Type Of Service Call
Installation
Machine
NFG/19-20/00085
Machine Name
A5598 JALANI ENTERPRISES HS WING DH SAF
Complaint
Type of Fault
Mechanical
Sub Type of Fault
Piston Filler
Make/Model
NA
Fault Characteristics
Checklist
Warranty/AMC
Call Status
Assigned To LE
Service Engineer
Not Yet Assigned
QE Status
Not Applicable
Faulty Part Image File
Not Applicable
Faulty Material Received From Customer
Root Cause Analysis
Select
aaaa
abcd
Abused by customer/ Process not followed
Auger center not done
Batch variation in customer product
Commitment not reflected in SO.
Commitment not reflected in SO. Auger center not done.
Component failure
Component failure. One of the case.
customer incoming power supply issue
Damaged in handling.
Design / BOM to be verified
Design issue
Design lacuna.
Direct material sent from supplier
Duplicate Complaint
Excess tightening of hardware
Failure Due to Overheating.
Hardware Failure
Hardware loose
Higher speed, Program correction.
improper / indaequate details in annexure
Improper packing of boxes
improper setting
Improvement point
Lack of effective process implementation
loose fitment
Machine sent on deviation. Machine dispatch urgency.
maintenance point not included in manual
Maintenence schedule not followed.
Missed during packing
NA
Non moving material used.
Operational wear out. Improper alignment.
Product at site is different than that given for demo trials. Change in product.
Product nature
programming error
Proper VFD setting not done
Quality order not assigned / removed.
Requirement out of SO scope
Root Cause Closure Not Required
Skipped from assembly person/not detected during trial at factory
Skipped from final quality inspector
Supplier batch issue
Supplier product quality issue
Supplier quality issue
Transit damage
Un-awareness
unawareness of programmer
Undeclared short supply
Under rated by design
Wrong supply
Description
Department
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Engineering
Finance
General Admin
HR
IT
IT
IT
IT
Planning
PPC
Production
Quality
Quality F
Sales
Sales Bangalore
Sales Chennai
Sales Delhi
Sales Kerala
Sales Kolkata
Sales Mumbai
Sales UP
Sales West
Sales West 3
Sales West 4
Sales-Hyderabad
Service
Stores
Supplier
Related to Food Safety?
Yes
No
Detectable
Non-detectable
Severity
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Critical
Major
Minor
6M Analysis
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Man
Machine
Material
Method
Measurement
Mother Nature
Type Of Concern
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Final Closure
Update Root Cause
View History
Back to Permanent Corrective Action
Permanent Corrective Action
Select
Checklist for trouble shooting updated
Design reviewed. Drawing & BoM changed.
Done counselling of concern workers
Inspection point added in FQA master white card
Long Term Resolution 1
Maintenence frequency defined
Maximum torque limit is defined and freezed
No corrective action required from factory
Other
Packing process modified.
Point added in machine manual
Procedure / guideline modified
Procedure / guideline prepared.
Procedure of inspection modified.
Production order ending will be done more carefully.
Shop floor process change
Supplier changed his design
Supplier process modified
Training given to designer(s)
Training given to inspector(s)
Training given to operators
Verification during assembly started.
Remark
Temporary Corrective Action
SE Remark
Root Cause Identified By